BONNEVILLE 2007
 
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This was a strange year. The SCTA/BNI crew that preps the courses did their usual trips in June and July and laid out three (YES, THREE) courses. Jim Lattin, the SCTA prez, urged the tech guys to find ways to get more runs out of each day and one of the ideas that came out was a three-course layout. Two of these courses would be long/short combo courses and one would be a shorty short course.
 
The combo courses would, when possible, run a long-course car then a short-course car, then a long-course car, etc. A new safety patrol position was created to declare the course clear after each run, obviating the need for the timing tower to verify this before letting the starter run the next car.
 
The shorty short course would be for cars that only needed maybe a mile to get up to their best speed -- oddly enough, there are quite a few of these.
 
But rain in July dampened both the salt and racer's spirits. It began to look like maybe Speed Week wasn't going to happen. In fact, some not-quite-correct info began to fly around the internet the week before the meet and I was seriously considering the wisdom of driving all the way from Texas.
 
We left anyway -- on the advice of friends who were up there, working on the course. Turns out that the course prep folks found some relatively dry salt large enough to build two combo courses on, plus the pits and tech/concession areas. And, in a matter of days, they did just that! I cannot emphasize enough how remarkable that was. And how grateful we racers (those of us who noticed) are that they put out this effort.
 
Before we left Seguin, I took the car down to San Antonio to get a chassis dyno tune. I was uncertain about the jetting and wanted to get some baseline for tuning on the salt. The first shot was kinda fun -- the Mustang went too fast for his dyno in 4th gear so I had to do the subsequent pulls in 3rd. And the car was way too loud for the other tenants in the building. Way too loud. But we didn’t get great results because the engine missed at speed.  Tried new plugs and plug wires but that didn't help.
 
I took the car home and made some changes -- changed some connectors and installed a new MSD box. Took it back the Saturday before we left (cuz the other tenants didn't open their businesses on Saturday). No change, still the high speed miss and no real indication why, other than some un-discovered electrical gremlin.
 
But -- the racing. Racers were able to put their cars in line on Saturday morning this year. Martha and I got out to the pits fairly early and hooked up our new towbar rig to the Mustang. Pulled into line and ended up #2 on the long-course side of the staging lanes. We have never been this close to the starting line before mid-to-late afternoon on the first day. Wow!
 
After the driver's meeting, we rushed to the car and I got into my firesuit and into the car. The car in front of us was having some sort of difficulty so the line steward had us push up in front of them. I was the first long-course car to run on this course! Wow, talk about a first.
 
The salt was pretty sticky on Saturday -- walking around you would pick up a wad of salt on your shoes like walking in sticky mud. That made the surface a bit slick, as was apparent as I ran up in the lower gears. I paid strict attention to the black lines and where I was on the course as I tried to build up speed. I also noticed that the high-speed miss was still there. After I shifted into 4th gear, I finally felt comfortable enough to take a scan of the gauges. Eeek! The oil pressure was down to 20 psi! I threw in the clutch, shut the engine off, and popped the chute. I had just passed the 2 mile marker -- and had clocked 173+ in the quarter -- but turned off just past the 3 mile.
 
We towed back to the pits and started addressing problems. I couldn't come to grips with the oil pressure issue so we took a look at the miss first. A friend of Dave Simard's, who had made the trip out with him from Massachusetts, came to the pits to help me diagnose the problem. We inspected the plugs and discussed jetting and such for a while. Then he started looking over the electrical system. Started finding all sorts of potential gremlins, including a loose nut on the charge wire from the alternator (drives an MSD box crazy), some suspect connectors, a loose fuse, and so on. And I thought I'd gone over the car at home. Color me embarassed.
 
After fixing the things he found (thanks to friends who came up to the salt to help with the car), we started the car up to see if it ran any better. While it was warming up, I noticed that the oil pressure gauge would periodically PEG, then drop back down to 40-60 psi. We shut off and I went in search of advice. The consensus was to inspect the oil filter and see what was there. I did and what was there was bearing material. Even copper flakes -- the layer under the bearing material!
 
So that was our run at the 2007 Speed Week. Not very impressive (though I can remember when a 173 mph pass would have made my day) but quite a learning experience. Guess I'm going to have to keep re-learning the adage that attention to detail is what separates the runners for the also-ran.
 
The best part of this trip, however, was deciding the next step just has to be a lakester. I talked with Russ and Eric Eyres about building a lakester starting next year. It will run the engine out of the Mustang, eventually. Shooting for 270 mph in D/L. Why not aim high?
 
Since we only made one run this year, we spent a lot of time helping out Jack and Warren Harvey with the SoCal Machine special, a modified roadster running a 254 cid DeSoto hemi on nitromethane. Jack set the record in E/FMR back in 2005 at 223 mph. He was hoping that Warren would be able to beat his record this year and join him in the 200 mph club. It took a while -- Warren seemed stuck at 217 mph for several days -- but he finally did it with a qualifying pass at 235 and a backup run to give him the new record at 232. We had to leave before he made his record runs but we got a call on the road from Christine when he qualified.
 
We blew the engine in the 973 car last year so it didn't make the trip to Speed Week this year. However, Aaryn bought a 2003 Focus SVT wreck recently and we are in the process of putting an engine together using what we can salvage from the original. We'll have a 6-speed trans this time, which should let us run the engine near the power peak better than before. So we should be back with this car in 2008!