2011


The Mustang is torn down with the engine in the lakester chassis, the transmission on it's way back into the 34 Cabriolet, and boxes of wiring and plumbing on the shelves. Our efforts this year are focussed on the, um, Focus. It spent some time at Henderson Performance Technologies in New Braunfels, being fitted for EFI. A BigStuff3 controller, 70mm throttle body, and a Hogans intake are part of the new configuration. We hoped that our mixture problems of the past were over and done with. 

Aaryn & I brought the car home on the Friday before we left. Had to finish up some items, like installing new seatbelts, installing a new lateral head restraint, etc. The entire family was here as well, so some social time was required. We pulled out for Bonneville on Wednesday morning. Thursday afternoon, coming down Utah Highway 6 from Price into Provo, it became clear that the brakes on our tow vehicle were on their last legs. Aaryn used his laptop and Verizon mobile wifi hotspot gadget to find Dodge dealers in the area and called around until he found one that could take us in right away. We arrived, dumped the trailer, and they fixed the brakes. New pads all around, new rotors in front. Sigh ...

We arrived in Wendover that evening. Out to the salt Friday morning to set up the pit area (thanks to Russ and Eric Eyres for letting us share the SDRC tent city they setup each year), and go through tech. As usual, the tech inspectors gave us a list of things to check out a bit more thoroughly; this year it was, thankfully, short. We spent some time hooked up the the EFI magic box, trying to learn how this thing works and how to download data. We thought we'd figured it out so we went back to the hotel for the evening.

Saturday morning, we drained the tank and went to the ERC stand for a sealed tank of 110 octane race gas. Then to the driver's meeting and then into line for the short course. (This year, the BNI volunteers really out-did themselves. They managed to prepare FOUR courses! There was the usual long course and then a combo long/short course, both starting from the usual place on the salt. Around the corner of the dike, there was the usual short course and then a 2-mile special course for vehicles that don't need 3 miles to reach speed. The lines were never all that long, even on Saturday.)

Our first run was more-or-less as expected. Nothing went right. The car was sputtering and not pulling well -- 131 mph in the last mile. We towed back to the pits, only to discover that we had no datalog either! (We eventually found out why this was.) Pulled the plugs to see if we could discern something about the mixture. Discovered, instead, that the ground electodes had been hitting the pistons and several of the plugs were essentially shorted.

This year we had finally gotten the correct rods to use the Arias pistons we bought two years ago. Seems they used a different rod length from stock and we didn't know that when we ordered rods from Crower. We ended up using some off-the-shelf JE pistons that year. Compression ratio was about 10.5:1. The Arias pistons give us 13.5:1 CR and, of course, stick up into the combustion chamber a bit higher. I didn't send any plugs along with the engine when it got assembled so no one had checked for clearance here. Ooops.

We ran into town to find some shorter plugs. The CarQuest in Wendover did have some shorter plugs -- way shorter. We grabbed them and returned to the salt to install them. Made another run and did, this time, manage to download a datalog. The car ran poorly and Aaryn turned out before the middle mile so we didn't get any speeds. Looking at the datalog, we decided to try changing the AFR from 12.0 to 12.8 and run again. Did so, with essentially the same results. Except I forgot to turn on the D/L and so we got no data at all. Back to the pits to see what was what. Pulled the plugs -- the electrodes were GONE! OMG! Ran a quick compression check: 210 psi on all cylinders. Thank heavens, we hadn't hurt the motor. The new plugs were clearly way too short and probably we were having pre-ignition on the exposed threads in the head.

Sunday morning, Aaryn went on-line to find a source of indexing washers for these 14mm, tapered seat plugs. Off to Salt Lake City to buy them then back to the salt to install them. We cut the gap way down (0.025") to pull the ground electrode in a bit, as well as installing the thickest indexing washers. Took the car to the Special course to make a short run and get some data. Aaryn ran 132 in mile 2 -- faster than any previous run. We pulled back to the pits to download the D/L and look at the plugs. No data in the logger! WTF? Turns out that the BigStuff3 datalogger has a "feature" imbedded in it; the data remains in the memory for only 30 minutes, after which time it is erased! I wonder who thought up that nifty feature? And who buried this tidbit of info way down in the manual? We saw that two of the plugs still kissed the pistons so we setup a new set of plugs with indexing washers and smaller (0.021") gaps and, for good measure, filed the ground electodes down a bit. Just to be safe, we richened the mixture some more by adding 15% to the VE table. FIgured it would be preferable to foul some plugs rather than burn something like a piston. We had more plugs.

Monday morning, we were in-line on course 3 right behind the record return-run vehicles, ready to run. Aaryn suited up, got in the car, and made it maybe 200 feet before the right side CV joint broke. Drat! We pushed him off the course and tried to tow back to the pits. Got a short ways before it became clear that I needed to go get the trailer. We got the car back to the pits, jacked it up. and pulled the axle. Yep, broken. Back on the laptop to start finding another axle. Aaryn found one at an O'Reilly's in SLC so off we went, again. Turned out this axle had the wrong spline count for our SVT transaxle. Off to Starbucks to regroup and continue the search. Aaryn was calling auto parts stores and Ford dealers while I was calling junk yards. The folks I spoke with kept asking why we didn't take it to CV Express and get it rebuilt. When Aaryn struck out, we looked up their address and drove over. The fellow there was unimpressed with our anxiety and told us they'd look at it in the morning and see if they had a joint that would work. They would "call us in the morning."

Tuesday morning, they did finally call to say the axle would be done in about two hours. So, off to SLC once more to pick it up. Lunch in SLC then back to the pits where we installed it. Aaryn was under the car, fastening the clamp that holds it in the transaxle when he noticed that the flailing end of the broken axle had punctured the oil filter. Crap! He called CarQuest in Wendover ... and they didn't have this oil filter! But they could get one overnight.

We had been in line with a pretty yellow roadster that was running a Zetec 4-cylinder engine too. So we thought we'd cruise the pits to see if they might have a spare filter. Didn't find them in the pits but they were in line on the short course. Ready to run, in fact. So we followed their pushtruck out the return road to see if they could maybe help us. No dice -- they didn't have one either. Nice guys from Colorado, first time with this car and they were having their own problems. We talked for a time and exchanged war stories about the Zetec, took some pictures. But ... we still didn't have a filter so we finally gave up and went back to the hotel. A gin-and-tonic and a soak in the hot-tub and pool, then dinner and bed.

Wednesday was the last day we had planned to be on the salt anyway (Aaryn had a business trip planned), so we checked out, stopped by CarQuest one last time, and hustled out to the salt. Pulled the car to the ERC trailer to buy oil, then into line on the short course. This time, Aaryn made it maybe 3 feet before the CV joint apparently broke again. Clearly, there is something wrong in the transaxle.

We had thought we had a fighting chance to work on Frank Sloan's record in G/PRO of 156.8 mph. And the engine seemed willing. As it happened, however, this would not have been enough anyway -- some folks from New Zealand brought up a beautiful Nissan with a very strong rally engine and clobbered the old record. The new record is now 173 mph!

We're back, unpacked, and mostly salt-free. Not very inspired to do much -- daytime temps of 105F are hard to take -- but we haven't given up hope. The computer says we could run 170's with 250-260 hp (we think we have 220-230 now, with the right tune). Pull the transaxle and see what is broken, maybe try the Texas Mile in March next year. Maybe ...

Later ... I found out what happened to the CV joint! I was looking on-line about solid motor mounts when I found a reference to something called a torque strut. Crawled underneath and, voila' -- a broken torque strut!

Torque strut

This explains why the engine could torque far enough to pull the CV joint apart. Took the car to Corey and he worked his magic once more. The revised and reinforced torque strut won't break now!